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”Intro Music by Karl Casey @ White Bat Audio”
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“All the videos, songs, images, and graphics used in the video belong to their respective owners and I or this channel does not claim any right over them.
Copyright Disclaimer under section 107 of the Copyright Act of 1976, allowance is made for “fair use” for purposes such as criticism, comment, news reporting, teaching, scholarship, education and research. Fair use is a use permitted by copyright statute that might otherwise be infringing.”
Follow on Twitter: @RainmanRay4Real
TikTok: www.tiktok.com/ @rainman_rays_repairs
Check out my Merchandise (because I don't say MERCH) for Men's and Women's Apparel, MUGS and Stickers! https://rainmanraysrepairs.myspreadshop.com/
Support the channel on Patreon: https://www.patreon.com/RainmanRaysRepairs
Patreon is a "Tip Jar" I don't post much there, daily YT uploads are all that I can manage for now
Amazon List, must have for any toolbox!
ATD Tools 13782 10-Piece Triple Square Spline Bit Socket Set https://amzn.to/3RV2fUB
Same as Matco. Mountain 5-Piece Metric Double Box Universal Spline Reversible Ratcheting Wrench Set; 8 mm - 18mm, 90 Tooth Design, Long, Flexible, Reversible; MTNRM6 https://amzn.to/3OJTRp2
Mercedes BMW VW Wheel Stud Master Kit: https://amzn.to/3OszRaL
Bahco "Frustrated" Pliers AWESOME tool! https://amzn.to/3IfDeOa
Brake Caliper Compressor: https://amzn.to/3gQBuiB
My Camera Gear:
Gopro Hero 10 https://amzn.to/3AaxELe
Gopro Hero 9 https://amzn.to/3EKDcM1
Hero 9&10 Dual Battery Charger MUST HAVE! https://amzn.to/3g5KdAT
Flexible Camera Mount https://amzn.to/3Jywrk5
#brakecleanmafia #wifeunit #rainman #comnissionearned
As an Amazon Associate I earn from qualifying purchases.
Also, I personally use or have used the products featured in my links and only recommended them if I feel they are of good quality.
”Intro Music by Karl Casey @ White Bat Audio”
Thanks to Jesse for making the intro and graphic for us to enjoy!!!
“All the videos, songs, images, and graphics used in the video belong to their respective owners and I or this channel does not claim any right over them.
Copyright Disclaimer under section 107 of the Copyright Act of 1976, allowance is made for “fair use” for purposes such as criticism, comment, news reporting, teaching, scholarship, education and research. Fair use is a use permitted by copyright statute that might otherwise be infringing.”
All right everybody, we're back to that blue. Jag One more time we're we're almost done fixing all the little quirks this thing has a showed up with over the past six months and I say six months specifically because there is a problem that I've been looking for for six months on this car and I finally figured out what the deal was. Uh, we had an issue with this where it would, uh, it would just intermittently not, uh, not have air conditioning I found a few leaks on it every now and then, recharged it. it seemed to be okay and I was never able to catch the problem and it's been sitting here for about a month.
I had this thing connected to life support. there were monitors on it, there were meters on it, there were test lights on it, and I continuously was operating the system on this car. The AC with meters connected to the power and ground going to the compressor and after weeks and months of trying to catch this thing in the act, it finally occurred and I was able to capture and prove that the compressor power was shutting down almost all the way it was going down, dropping down to like four or five volts and all of a sudden it would work again and I would check it. We'd had 12 volts just like our battery voltage like normal and it was.
it was only happening for you know, 15 20 seconds after startup, then it would go away and then there was no problem. I've been into the dash on this car and I've been monitoring the HVAC control unit which was a up under the dash right here. it's way in there and I had found that uh, the HVAC control unit had stopped. there's wifey in it, it had ceased uh to supply power to the compressor and it was doing it very, very intermittently.
Again, my problem was I could never catch it in action. Watch. she's gonna park right in front of me. Don't don't park here.
No. keep it moving. Keep it moving. Don't park here.
she's gonna. She was thinking about it anyway. where was I Okay, so I would I couldn't catch the fall in action and again I continued to monitor the compressor side and I would monitor uh, what the voltage is and the grounds were doing at the control module. See, Uh, once the system is commanded on, the control head tells the control module to power up the compressor and then it sends power to the compressor.
Then the compressor kicks out and does the thing well. The issue was is when it was sending power down to that compressor intermittently, it was only sending out about four volts. So you're going okay. Got it? No problem.
Looks like we have a a bad HVAC control module. so I ordered a new one. Now I've got this thing about replacing control modules, especially control modules that have been in service for a very long time. Usually they don't fail on their own.
Something causes them to fail. So while I was waiting for the replacement control module to arrive, I continued to test and monitor the system because I knew I was on the right track and I knew I was narrowing down what the deal was. So what I did with the system running is I waited for the fault to occur when it occurred. I supplied 12 volts of fused power directly to the compressor and it was blowing up the fuse. It wasn't doing it consistently and what I had found is that the circuitry of the control module was affected uh by The Fault in the compressor. So I I do have a control module in there on the shelf and I've got a compressor that has been ordered. it's on the way. I'm going to change the compressor first and then retest and if I find that voltage being supplied to that compressor is intermittent or it's dropping below you know, battery voltage or 12 volts something like that while running, then I'm going to go ahead and toss in.
Uh, toss in that other module and I know what you're saying. you didn't record it so there's really no proof and and you're kind of right. But like I said, this is a month-long uh Endeavor of me trying to figure out what the deal is and I was actually kind of annoyed once I found out that the compressor was faulty. Uh, for a couple reasons.
Uh, reason number one is this compressing unit is uh, it's about a year old I I did not install this, somebody else did Once Upon a Time it's down there somewhere. but uh, you know we were always operating under the assumption that we have a brand new unit here and I forgot to remind myself that new does not mean good. It means it's not used very much. So let's restart this engine.
Let's power up the system because I found another symptom that we were overlooking again because Hood Gravity re-popping Z Hood Because we thought that the situation was a power steering concern, not an AC concern and it's not doing it now. but intermittently. One of the complaints was is on. Startup the power steering pump was making like a a grinding whining type of buzzing noise and again it was only occurring for a few seconds and then it would go away.
and I found out while I was tracking down this compressor situation that it actually was not the power steering pump, it was in fact the AC compressor also making that sound. I've never heard compressor make the sound that this one was making and I wish it was doing it right now, but it's not. Maybe it'll start winding when we get inside. but regardless, I've got one two I think three ways that uh, I have condemned this compressor.
So we're going to go ahead and get this thing up in the air, pop that guy out of here and uh and get it replaced. So stay tuned because this it's probably gonna be the final video on this. Jaguar because I fixed everything else once I fixed this. It's good actually I lied.
There's also an intermittent check engine light. uh I forget the code. uh, the code says something about fuel rail pressure is too high. It's telling me I have too high fuel pressure I've already verified the wires and I think I put a pressure sensor in at once upon a time. but uh no no no no, it was a fuel pump because I had low fuel pressure I Remember now but yeah, it's got a code intermittently it says fuel rail pressure is too high I'm not sure what the deal is with that. I've uh I've been stumped on that one for a long time as well. Um, any Jaguar guys know what's up with the too high I feel raw pressure on uh on the old Xjs. Let me know in the comment section.
Anyway, that's enough fishing for uh, viewer interaction. Let's go ahead and get this thing in park and get started powering down. Let's see. So here's our compressor up here.
We can see it's a fairly newish. uh, there's that connector. Um, yeah, so this is gonna be fun to extract because it doesn't come out this way. It can't go up because there's other stuff in the way.
so it's obviously got to come out through through here somewhere. I'm probably gonna have to pull the subframe down some to get some space. Um, this will be fun All right. Well let's pull the wheel off and get started.
No sense I'm staring at it. It's not gonna get fixed that way. once I start moving like a diesel. Hard to get going.
but once I'm there I don't stop. Nuts are swollen. There we go. Step one complete.
Come here. Okay, it's become very clear to me that this fender liner thing has to come out at least I hope it does because I'm taking it out and if I take it out and find out I didn't have to take it out I'll be sad that I took it out. Shoot rambling on that big one didn't fit I need to get the middle one out. Where are you? Yeah, it's held in with a bunch of these little plastic push Clips Okay, now in typical uh European Vehicle fashion, we've got some Torx Fasteners mixed in with the the plastic connector clip things here.
and why do we need torx bits in lieu of plastic connectors? I Don't know, but we got him and a washer. you know looking at this in Greater detail I uh I think I don't have to remove this at all I mean I'm not going to gain much space by pulling it out, but I'm just gonna go ahead and finish it off. I See no reason to back out now from here. Oh, another washer.
Yeah, someone's been here before. These washers aren't supposed to be. You know? back you guys up a little bit. let's fish this thing out.
I Got a text message. that's why the radio stopped come out plasticky bits. There it is there you go. Step that down right over there.
Perfect All right, we're moving back up to the run of the engine here. We need to reach up in there and get a tool on that belt tensioner and go ahead and pull pull that loose so we can get the belt off the compressor. So what? I'm gonna do stick this guy up here and see if I can't reach in and plug in the ratchet to the the drive thing on the tensioner. It looks like we got it.
and yeah, it goes that way counterclockwise. Lefty Loosey Tensioners on tension and I've got the belts off of the compressor. There we go. Okay, let's move back into the wheel well and work on those lines next. Actually, I think I'm going to work on the subframe next because I can't even get to the bolts. See that right there? That bottom bolt that runs right into the subframe. So yeah, I got to pull this up frame down just to uh just to get the scene to come loose. So let's uh, let's do that next there.
there's one of the mounts for the subframe there. Let's get in with the now with the angular impact and pull that bolt down. I'm gonna try to do just the two on this side and maybe the thing can just lean down. It's kind of the idea and we'll see how it works out.
Okay, that's in. Let's get the other Mount over here down right there. I Think we're looking at 15 millimeters because the engine came down with the subframe. but we did get uh, more space over here.
so I can squeeze this thing through. I Think let's get uh, let's get the jack stand and take this down as far as we can. It's good. Raise this thing up some all right that's gonna hold the weight.
then I can pull the rest of those two bolts out and this thing will be free from the frame on this side and we can try to maneuver it from there dirt. Cascade A big bowl? Let's see. I can pull this one out the rest of the way. now.
come here. Seriously got it. You go over there next to your brother and all right, we'll pull this guy a little bit looser. Okay, it's not gonna come down anymore.
That's all we get me. They got to disconnect the strut. Hey, let's go up here and pull these. uh, these little nuts out for the strut.
See how this drive went down? Let's see how far we can go with this one. Let's see, we'll put that one on Three turns. Pull this guy out. That's about all we get I don't want to go any farther actually I don't think I have an option I need to pull this out the rest of the way.
Uh, let's remove this connector if we can. Yeah, that was easy. Came right out Okay, oh, let's let her down some more. That's about all we get.
Yeah, it's uh, it's done coming down. Hope that's enough. Okay, so since the subframe is now lower, the engine is now lower which does not give me any extra space. So what I need to do is keep the engine up higher and then get the subframe lower.
So I will now unbolt this engine mount from the subframe, down through that hole right there, or up through that hole. and then we're going to use another jack stand to push the engine up so I can create some space here. Fun clicks, foreign. So what I'll do is I'll move this stand over here to hold up the engine and that'll let me lower this stand down.
If I can get this right, clearances and whatnot, you know that should be good. Okay, engine's going up. subframe is staying down. Now we're talking. Hey look there's that bolt that I couldn't get. It's coming into position a little higher. This is a this is weird. There we go.
See that. All right, 10 millimeters we have contact on clips. haha. Yes, Finally, we're getting somewhere.
don't know where we're getting to, but we're getting there. Hey, a nut fell out. That was weird. Anyway, there's my Bolt look at that.
The nut that fell out of it has got half of it ground down. See that I don't know if that's Factory or not. that's I've never seen that before unless someone did it deliberately. Okay, so I've got the bottom bolt out.
Let's let. uh, let the engine down, keeping the subframe also down and we're gonna go down as far as we can until I can reach the top bolt and the back. Bolt for the compressor. Okay, now the there's another bolt back here.
There's I think there's three for this compressor. Third one's in the back. Oh what? That one's not even tight. Let's see it.
You can't see it steering on here there. Now you can see. Look at that. that one's not even tight right there.
It's just. uh, we be wobbling. Hang on here. let's get that thing out.
Well, the situation is not not boating well for this last installer of this. Okay, okie dokes, we've got one more. one more Fastener here that wasn't very tight either. Oh the shame.
Wow, really Here it comes here. It is all right. that's three bolts. This thing should be free.
Yeah, nope. stuck pry bar. Just get behind it here and try it towards us. I'm sure it's just got some alignment dowels or something to hang on to it.
There you go. Okay, now, a little higher up we've got the two connections for the hoses. Those are gonna be fun. Yeah, you see them up there on there and one over there.
I've got to reach up with a wrench. you know, get those disconnected. Okay, we're going in Long Reach with the ratcheting wrench. Hoping to get a hold of these these bolts up here.
unless I have to get them from the top. That's a tight squeeze up there. super duper tight. Yeah, that one's loose.
I'll be able to get it out, but you guys aren't gonna be able to see trying again. I've got my little stubby ratcheting Crow's foot little device. that's enough to get some turns out of this thing removed. there.
It is all right. So that's one of the bolts for one of the lines, which they're both under vacuum right now so those don't want to come out. Okay. going in for the line number two.
that one's actually a little farther back than the one I just did. This is really fun. I can't even see what I'm doing and I can't get this from the top. There's like no visible access here.
This actually sits under the V of the engine. so if the if the V is going like this, the compressor is down under it. so I can't get a any line of sight at all. Okay, got a wrench on the bolt that was took some finesse. all right, unclear. Okay, yeah, we're getting somewhere now. It's loose. Come on.
Jaguar Yeah, that Line's gonna be fun to put back together. I'll tell you what. I can't even get tools on the bolt. You know this kind of stuff wouldn't be so bad if you could fit two hands in these positions.
You kind of can't see super duper no space here. All right man, it's got to be close. Come on. Yeah, there we go now.
I got two fingers on it. I will defeat you and now I figured out how to put it back together too. All right, there's the bolt right right there. Got it all right going in.
Let's go ahead and get these lines detached. They're only being held in place with vacuum from the recovery machine. I can just get under it with this little pry bar thing here. it'll pop up there we go.
There's one pry bar for everything. that's line number two. All right. So it's free.
Unit is now free. It's just kind of floating around in here now. I just need to maneuver it out. That's the next challenge.
I Don't know a little bit more up and I think I got enough to get this out I think because here's the tightest of all tight squeezes. I think I've got over here on the left I Pry barred the subframe down and I have a socket wedged in here there. Oh, you can't see. there you go.
There's a socket in there. stuck pry bar right here. pulled this thing down, stuck a socket in so it's holding the subframe down. the engine's being held up and I think this is enough to get this thing to come out.
I think I hope because if I'm wrong. uh I don't have some problems here I might have to pull the sway bar out. No no no I got it. Yes, she's out.
Uh, what a relief. we're getting somewhere to the bench. Let's go check out. uh, this unit compared to the new one.
I'm sure it's gonna fit and we'll get this guy installed. This is a faulty, newish compressor. Very unfortunate. Get this stuff over some tool gravity.
No worries, it was just a 10 millimeter foreign. Our mounts look the same. there's three, our connector is the same, and our manifold and ports also look like they're the same. So what? I'm going to do I'm gonna go ahead and pull these bolts out of these ports that way.
I Don't have to worry about it later. Pop this guy off. pop. Okay, set that right there.
come out okay. Come on. New compressor coming with us. See how this is gonna work here? Get it SPID back into its home here.
same way the old one came out, which is opposite of what I'm doing. Yeah, hang on. we're doing this fast backwards. I Think the the spinny end came out first.
Let's try that. I Honestly already forgot. it's been like 45 seconds and I forgot it's been a long week. I know you go in there.
so let's just get with the program and do what you're supposed to do. Come on so close right here and there's alignment dowels in the bracket that are going to hold this. Yep, right there. That's where it goes. Nice. Okay, before we get all excited and bolt this in I Want to get those lines installed so we're gonna pull little plugs out of there and get the lines fed into position here again. Yeah, y'all can't see what I'm off to. it's too dark.
super dark in fact. I can't even see what I'm trying to do. Where's the hole? I See it. There's a hole for the a, uh, a roll pin and sticking out of this compressor.
and I'm supposed to line up that roll pin with the little manifold flange on the hose and that's what sets the alignment. And naturally I'm having a hard time getting that to a lineup because because Jaguar and I can't see it because it's on the other side of the unit here, I'll just keep wiggling it. it'll go in. Okay, so it's it's lined up.
but uh, the roll pin will not press to that little flange. So I'm gonna put the bolt in it and start the bolt and hopefully that bolt will, uh, will draw it back down. No space at all to work with. this is so agitating.
You know it's not really that bad. I'm just kind of grumpy and fatigued from earlier operations that I was conducting this week. Okay, the bolts starting. We're going in.
Okay. this is going to take a while. Isn't it all right? It's getting smooth now. it's starting to slide down over the PIN.
You guys can't see the pin. Like I said, it's on the back side. but it's going. Let's keep drawing this down.
Okay, let's finish that one off with the larger ratchet. We're almost bottomed out. I'm running out of flangy strength here. Foreign.
Okay, let's finish this off with the full-size ratchet. It's a it's almost bottomed out and I'm having a hard time turning it with the little finger ratchet. so we'll get this big guy in. Ah, Blinded by the Light too much lumens? Yeah, let's see if I can just get if I get a finger on it through here I can hold it I'll bear hug it again and try to bring this.
uh, up the torque here. it's gonna take a while. slow and steady. a couple clicks at a time.
Not fun. Come on. AC Hose: it's almost there. Come on a little bit more Raw and one more pull for good measure I Know you guys can't see I'm really sorry.
stick that has one hose installed. Let's get the uh, this other one installed and then we'll bolt this thing to its bracket. Here's our plug, one down, one to go. Let's get our little Peg lined up and then we'll get the big Peg lined up and we'll get the bolt in.
These angles are all weird here and these hard lines are not very forgiving. They don't really have a lot of motion. There we go. Now we're lined up.
kind of. Yeah, buddy. That's it that went in All right. another 10 millimeter Bolt Slide that guy down, get you started. Oh good. That one's going in a lot easier. I Don't think you can see? Nope. I can't see, you can't see, We can't see, but we're all in this together.
Unless you click away, then you'll be somewhere else. That would be bad. Oh, come on with it. All right.
that one's down. A little bit of increased torque on that so it stays tight unlike the mounting bolts. Oh, it takes and take this guy and put it back up in its position on the bracket. That's a flashlight.
Saw that coming. Yeah, there we go. Put our illumination back up here. These just stay right there.
Okay I don't remember. These are all three different lengths. All right. this is the bottom one because that's the one with the little shaved off nut that probably isn't supposed to be there.
I would be. uh, willing to wager. Threads and the bracket are stripped, reaching around on the back side to get that nut on. Yeah, those threads are stripped out.
This bolt doesn't even go here. it's too long. Okay, next one that's going up top. what are we doing? We'll push it in some wiggle it.
it doesn't go wiggle it and then it goes all right. wobbly 10 coming in kick, two clicks and where's that other last little bolt that I do. It's in my pocket. Run this guy down.
Yeah, that one's stripped. All right. That's why it was loose. it's stripped out.
Cool. Why? All right? Well, what do I do about that? Let me see. what do I do I Oh, that's not okay I don't have a uh I don't have a way to put a Fastener on the other side of this stripped out Bowl right here. And this is kind of important because it's the only one.
Hmm I think of something here. Oh I know I know what to do I have an idea. Okay, here's here's my solution: Some grease and some wire. The grease is to make the wire stick to the bolt.
I've got the end of it bent down so I can get it to go into the bolt hole and I'm failing. and I'm basically going to wedge this bolt in between the stripped out threads and the bracket and in between these pieces of copper wire. What it's going to do is it's going to smash that wire down and then it'll be able to grip remaining surface inside of that bracket. That's the plan here.
so you're going to work or it's not. and if it works, we're in better shape than what we started and if it doesn't work, then, well, we're in the same position. So we're gonna put this thing in and send it very carefully. I Don't want the wires to come off of that little bolt there all the way in.
That's it. All right. This might take a couple of attempts, but it's better than nothing going. haha.
Hear that thing bogged down. It's working a little bit more. Click? All right. That's better than nothing.
It's got some clamping force on it now. Sure, let us proceed. Thank you. We'd get the connector connected.
That's easier from up here than it is down there, that's for sure. And I think this clamps on somewhere around here I Don't know where. Um I figured it out. There is a there's a bracket on the old compressor. We'll bolt that thing onto the new one and then use that bracket to secure connector. I Think that's how we're supposed to do this. That guy down right down. Come tight please.
thank you. Then this. You can plug in and look right here. Yeah, that's how we do that.
Look at that. That's nice. It's much more better. We'll snug down that little bolt with some eight millimeter action.
Foreign click. All right. Well, while we're here, let's see if I can't get that belt in position. let's see there.
reach up. Pretty sure I can get it on from where I'm at. I can give that uh, that ratcheted tug and untenching our tensioner here to miss. All right, belt's on.
Give me back my ratchet. Got it ratchet recovered? Uh. visually inspecting the belt. it's on all the ribs.
That's good. Okay, let's get out of here some and pick the subframe back up and get the engine bolted back down. I Need to unpry Bar my socket. See you right there.
We're gonna get under this guy. Give it some down socket recovery. compete. It's like a another bracket stabilizer Mount thing.
Jaguar stuff. Who knows, bro. All right. Big Bolt Coming in, let's get all this stuff lined up better.
line up. Yeah, it's a little. it's farther back than it needs to be. I'm gonna let the engine down onto the subframe and I'll bolt that in next.
I think and then I can pry bar the subframe forward and get that hold of mine back up. All right engine is now sitting free. let me run the bolts in real quick and then uh, we'll go back to some pry bar action. now.
where are you wait in there? All right Motor mount clicks. that one's in. Oh, curiously enough. I uh I Checked the other side and found out that the lower bolt was missing.
So I uh I find one to put inside of that too. There's a not missing for the motor mount. anyway. I'm gonna raise the subframe up some and we should start to, uh, see this hole become aligned over here.
I think a little bit up a little bit more up. Yeah, there we go. Get that. AC line out of our way.
not up enough to start the threads though. so up a little higher is that gonna do it? Nope, it's close. Let me try the back one and here let's see if I can get this back when we go in. Foreign yes and I need to re-tighten this one now.
Can I get that one to go in? Let's find out. Survey says yes, it is threading now. Good foreign. Let it move around a little bit.
Get in there here. you guys wait here. I Can't reach that stupid thing. All right? That's all four subframe bolts.
Good to go. How are we looking Tight? That's tight. Compressors in belts on. Okay I need to go up top, put the strut bolts in and while we're up there. I'll pull this thing into a vacuum so I can recharge it later. see I Don't think we need these anymore. Right out of here. Let that one down.
get you out of here. Very good. All right. Moving back up all the way up.
Let's get these nuts back on the strut at these. Got four of these guys. Oh fail. look.
I grabbed the wrong electron clicking device I have too many impact guns. Now that's gravity. That's a lie. You never had too many hot guys and we shall not neglect the connector for.
The Airliner Whatever this thing is, what are we doing and why are we doing it like that? It's problem here. There we go. It takes all right. system's vacuuming.
Let's pick up some of the mess here. I'll let this thing down a little bit and then we'll get that fender liner reinstalled. All right. Let's check on our machine.
Uh, 2.5 minutes remaining. I'll be back in 2.5 minutes. Don't go anywhere. Okay I actually lied, it's been longer than 2.5 minutes because I was inside of the cabin.
uh, putting all the paneling for that computer module back together. So uh, let's just go ahead and fast forward here and charge this thing. I believe it takes 1.4 pounds refrigerant it's not electronic and then we will stop to use the engine and see if this thing's gonna work anyway. I Want to see if that stupid noise is gone? I Know we didn't hear it when we drove it in, but I've been hearing that noise for like six months.
Foreign refrigerant on the high side? Please send it full send. Let's do it. You gonna go? You gonna go? You gonna go? You're Gonna Go You gonna go? Are you gonna go? It went all right. Okey doke.
So the machine just beeped so it has completed its recharge. Let's restart this thing starting Z engine and powering on AC As soon as the controller is done. that's good. Oh, we're already getting temperature drop.
Awesome! Let's go check our gauges. That thing came on instantly. It usually took a few seconds and then it would come on. Yeah, pressure's coming up.
good. Pressure differential. Okay, this is gonna take a little bit more monitoring just to make sure we're good, but I'm not hearing a groaning noise that I heard that we thought was a power steering pump or or an air pump. It's not doing that so it came on instantly.
This is good. Pressures are good. It should be making cold, but that's not a good mate measurement for the day because it's kind of cold today. But yeah, we're already down.
Well look at that. it hit 40 40 degrees fast. 40 is the green right there. A little green little Notch I don't know if you can see it, there's a glare.
Yeah, this thing hit 40 degrees Fahrenheit quickly. Wonderful! We're good to go here. I'm pulling this for the success finally. Uh, the only thing I have left to do in this car is get a replacement uh, sealed for the bottom of it which I could do that later. So uh, all that being said I'm gonna go ahead and get my machine back and we're gonna go ahead and uh, button this thing up I'd really like to get it back to the fella that owns and he misses his Jaguar So all that being said, as always, just like, thank you for watching this video. hope you enjoyed my video. If you did enjoy this video, please feel free to let me know about that in the comment section down below. Tap that like button while you're down there.
And most importantly, do not forget to have yourselves a great day! See you guys later in the Jaguar.
4 days after this was posted, Lauren had not seen nor heard about the video. Ray might have had time to create a good reason.
Hood gravity… This will never be accidentally filmed again… Perfection.
You love your job so much; you do poo you don't have to.
Maybe I should try some of those gloves. Trouble is, I'm so used to seeing blood on my hands. I dunno. Need to think………………………….
2008 Jaguar XJ is a Ford Motor Company design… They sold to Tata in 2008 but the XJ series your working on is a FoMoCo product. As is normal for Ford, they cheapened the cars so much, they all but killed Jaguar as a brand… Because American drive for profit over quality. They're absolutely covered in Mondeo bits (I'm not sure if you got Modeos in America, dodged a bullet if you didn't. Awful things, they're only redeeming feature was the Sony stereo in the dashboard.
You do like to do things the hard way, and take twice the time, lol. Is that for extra drama, in order to increase views on YouTube, or just so you can charge the customer 2x labor?
Holy Subliminal Wife Unit referrences, Rainman!
I am a long time Jag x358 owner. I went months of experiencing fuel related codes that would wildly come and go and got progressively worse. I would get a fuel rail pressure fault but checking the schrader valve always showed normal pressure.
I eventually figured out that the sunroof drain tubes became blocked and water would come into the cabin behind the dash and was dripping right on top of the main computer behind the glove box.
You forgot the X-Files music when your daughters was seen, which as a X-Files fan enjoyes.
Did new o rings go on the lines?
Ray you didn't change the schrader valves again. This has been tough on the customer already, hope he doesn't have a leak in the future.. P.S. still love ya 🙃
About the diagnosis…for a minute I thought you altered the situation by monitoring.
I once spent days catching a faulty webserver in the act. I just wanted to get a timestamp of the failure and so i could analyse the logs. While monitoring it never failed! I monitored by constantly asking the webserver stuff. Apparently someone thought is was a good idea to suspend one of the webserver processes when it was unused for more than 24 hours. By monitoring I kept it from entering sleep mode.
There is no way my ham hands would fix in there.
I've had to borrow my wife unit's phalanges before for tight spaces like your in. Smaller hands for the automotive engineer's smaller brain.
I’ve used that wire method before and it worked for me.
Welcome to the world of English and German cars , constant problems.
Is it possible the stripped bolt holes may have contributed to the compressor failure? Or is it more likely just a faulty unit that was installed?
you got me! made me laugh with the wipe pic
fuel rail pressure high had that and 25 other codes in my Peugeot 308 , think it was fuel pump damage causing metal into some sort of pressure relief valve , but I was getting both to high and to low
Where you get the mini lights from the block ones
Brave!
Re: fuel pressure code. Some jags have a known issue with leaks and faulty components (specifically a faulty pressure sensor and regulator). Some of those pressure regulators are solenoid based, so if they stick they don't work correctly and cause fault codes. One owner reports replacing the solenoid coming off the high pressure fuel pump as their final fix to it.
I do love a good jaaaag!
In my experience the fuel pressure regulator doesn't last all that long. I've had my XJ for 5 years and have had to replace the regulator twice.
I figured it out as WELL. It is a Jaguar
Honestly, I've had an intermittent issue like that and it ultimately was the fuse itself. It looked good, tested good, but only after saying eff it and replacing it, did my issue get fixed. Nowadays I replace fuses like you do AC Schrader valves.
Don't forget to take the transmission out to change that air compressor.
I worked on a few Jags back in the 80s at a Triumph Stag specialist. spotted the fault right away when you opened the door – the steering wheel is on the wrong side. Jags never work properly like that
i am sorry i will not do that job take it to jag..
There is a very easy explanation for all the problems you have with the Jaguar: It's a British product!
Ppl, it's a FORD. 'Nuf said!!!!
Never seen that copper wire in the threads before, that's like something outside of redneck injunuity carpentry class👍
My wife had a 2002 Jag XJ. Most miserable POS we've ever owned. Most of what was wrong with it was above my knowledge level so I kept a local shop busy working on it. One of the happiest days of my life was watching it drive off into the sunset.
Awesome 😎
I’m just throwing this out here. Do you think that was a ground problem because of the loose bolts
OH. THE SHAME. Is that a line from Apocalypse Now movie?
I was at a Jaguar meet one day, sat having a drink and chatting to some folk. One of them proudly told me that he worked in the design office. He showed me his phone and pulled up a couple of 3D renderings of a fuel pump that he'd recently completed the design on. "So what consideration do you give for future maintenance, access and the like?" I asked him. I was greeted with a blank stare. "You know, how does a mechanic access that pump if it fails and needs to be replaced?". Eventually he replied… "Well, I wouldn't know, I don't work on the shop floor".
Wow, who would have thunk….an English car with an electrical problem.
and you never changed the line seals
I was informed years ago that if you purchase a Jaguar, you need to buy two. Because one of them is always going to be in the shop.
Time to designate a wife unit parking space!!!!
That right there!! Is why mechanics make better lovers!!
😏😉😄
Sorry Ray for a thumb down, I removed it but not sure if it was taken away.
Was trying to like blue towel video and it reloaded just before pressing thumb up, and it's directly in same spot
always enjoy your uploads thank you Ray.👍👍
Hey ray where did you buy the Black Lights that u hang on a charge station
I have found that the best way to cure driveline problems in a Jaguar XJS is to replace the drive line with a GM 350 engine and TH350 transmission. Clears all of those weird Jaguar engine problems RIGHT up!!!! Also, it makes it easier to find parts for it when you are travelling in the middle of the American deserts.
There used to be a kit for this back in the day. Don't know if they are still around (haven't bothered looking it up just for a joke 🙂 )
You certainly earned your money on the job. A bit of a pig to work on.
You taught me something new with the copper wire trick!
"Better line up… Hmmm…" 😂
Ray I hear the Doodly Doo phone in the background lol
no swearing?! you must be an enginegynokologist !
Good morning Ray I m sure when you find lose bolts you think there could be other problems from the replacement compressor I m sure after you’re done it will be fixed right with tight bolt Thanks for the video
F'n fantastic!!!! Nothing better than fixing a long term issue!
I've always heard that Jags are prone to errors and hard to work on. Thanks for confirming it.
Imagine doing that job with no lift
Wow that is such a lot of work to get at the part that had to be replaced.
What happened with heater control?
If I was the owner and watched this video, I would not pay for that caliber of work, wire and grease to fix a stripped bolt? Why do we think the old compressor made noise? Damn Ray, you really shocked us on that Jankey repair!
Run a tap in the whole! Oh my gosh, shade tree for sure. Grease and wire. You have to be kidding me? On a Jaguar? Jankey as hell!
Great job Ray. Loved the way you stayed with it to diagnose properly. One comment: I noticed the blue locklite on the strut nuts that you didn't replace. 😉
I can't believe as hard as that unit is to replace, WHY WOULDN'T you replace the Oings? WOW WHY WHY WHY! Damn Ray. I think you know better, but why would you risk a leak, or maybe because it wont leak for awhile? Man Ray, you should know better! In my 42 years, I have never installed a A?C component without new Orings or seals. Another comeback we wont see, or the guy will probably take it somewhere else.
Workbench is a reflection of the mechanic is what I have has heard! LOL
What happens when the flange on those lines get bent by prying on them< Asking for a friend!
The stripped out mounting bolt, along with the loose bolts probably caused the grinding noise and allowed the belt to slip causing both of the AC problems. The shame is on the previous mechanic.
I sure hope u used new rings.
That strut really helped? lol Maybe ALLDATA would have saved money on labor, just saying! Nothing wrong with research, sure better than just winging it!
Why not research thru your ALLDATA, before starting a job. It will show you what has to be removed. Seems you think it is easier just to take everything off, or unnecessary part removed eats up profit!.
I feel sorry for that customer!
Power steering sound was A/C compressor? First I ever heard that one1
Why didnt you film your diagnosis? I would love to have seen that! Why change compressor? Because we aren't sure what it i
I just love when new(ish) parts fail. That makes me almost as happy as people that cut me off when there's no one behind me just to make the next left when there's a long line of oncoming traffic. Needless to say the words come out of my mouth is enough to make a sailor blush.
I am now VERY happy that 20 something year old me was not able to afford the Jag I had a chance to buy around 15 years ago… Looks like it could have been a nightmare if it ever broke down!!
A little birdy tells me you might have a new employee?
Hey Ray if your having issues with fuel rail pressure too high, well first has the pump been changed? Unless I'm mistaken, this is a returnless type system, with a pressure relief valve built in the pump itself. And they are known too have issues, you might try using something like shop air to pressurize the pump/system (through the schrader valve) and see at what pressure the relief valve opens, and if it causes the pressure sensor on the rail to hit 5v then it is not calibrated right, and it needs another pump.
This right here furthers my reason for not wanting to touch a Jag… I don't even want to take a test drive. Might blow a code just by breathing in it.
It will be back next week wih a broken timing chain tensioner. Another 3 grand to repair. We used to call these an all day sucker.
most excellent
Reeeeeeee
Totally awesome job Ray even with frozen nuts
Ray I have seen the SAAB on the transporter. A older 93. Get your TECH 2 out Ready Ray. It looks nice. I have a 2007 Convertible 2.8 V6 GM engine Aero Anniversary with only 3,864 miles on. Still running original brakes etc. Heated Garage all its life. My Wheelchair fits in it, Best Car I have had, Best Seats for my Spinal Injury. Keep Saabs alive Rainman Ray. Thanks for your Videos they KEEP ME GOING ❤👨🏻🦳♿️🇬🇧🇬🇧🛠️👌👍
Mr Sublimal
Ray:
“Ahhh! Blinded by the light”
“Too much lumens”
Me: “copyright strike”
MAN ….what happened to just a switch
That era Jag is the same as Lincoln LS.Frp circuit high I always replace the pigtail.
Showing pictures of The Wife Unit whenever you say the word whining. She could see this Dude, do you have a death wish?
Excellent say hello to puss from me. Done the stripping thing myself. Copper wire next time bent over at the end. Cheers 😎
I found a new nickname for Ray , his name from here on will be "GOLDFISH" because he has the memory of one as he forgets things in 45 seconds.
Nice work! You did well to find that fault being it was intermittent. I've never seen a variable displacement compressor valve do that. Usually jam up and sometimes open CCT but an intermittent short is like winning the lottery. Again well done!
A month?!! Shoulda called a real mechanic for advice, like Eric@South Main Auto! Boom!
Ray you made your own Helicoil with a piece of copper wire. That is a working person solution when they do not have time to go to the store to get an actual Helicoil.
Awesome troubleshooting, Dude!! I'm a retired computer programmer, and I would set up data dumps to catch an intermittent fault in end of day processing. The satisfaction of the fix is unbelievably satisfying. You ROCK!!👍👍👍👍👍
Come on Ray… the you'll never hear the Brits say "Jag war"… What you hear, is that they say "Jag you are"…. short on the you… but the you…. is what is required to make it sound right 😉
IMHO…. My 1986 XJ was the last, if not the sexiest jag ever made. The curves of the body work on that car… were… quite frankly… volupuos.
Hand washing around the curves of it's rear end…. and the curves over the head lights of that car … if you let your mind roam…. oh my!…🥴